Site 2.23
      
            Site ID
          
          
            2.23          
        
            Health
          
          
            COD
          
          
            2017          
        
            Nominal Capacity
          
          
            348 kWp
          
        
            Average Specific Yield
          
          
            1324 kWh/kWp
          
        
          Total Estimated Loss
        
        
                19.72%
        
      
          Possible Gain
        
        
          6% to 10%
        
      
          CAPEX, OPEX
        
        
          1.01 ₹/Wp, 0 ₹/Wp/a        
      
          Expenditure / Energy
        
        
                      0.6 ₹/kWh to 0.4 ₹/kWh                  
      Abstract
              Several modules with cell breakage and isolated cell parts were detected. Cables and connectors were exposed to ambient without any UV protection, they also display signs of abrasion and cuts. Several clamps were improperly fixed, and many were faulty. It is recommended to (i) optimize the cable layout (ii) replace rails that offer better ventilation (iii) restring the modules with cell breakage, and shaded module to dedicated strings, and (iv) install a weather station or at least an irradiation sensor to monitor performance ratio. The estimated production boost expected by the retrofitting actions lies between 6% and 10%.            
                          
                      Main Findings
                          Poor cable management: Cables and connectors are degraded from exposure to ambient conditions. The cables also showed signs of abrasion and cuts, and low bending radius.                        
                      
                          30 mm rail used in flush mount causes higher operating temperatures.                        
                      
                          Open shaft holes found on site.                        
                      
                          Walkway installed over landscape module, casting permanent shading on the module and reducing string protection.                        
                      
                          Clamp fixations at several locations show improper application leading to misalignment and imbalanced loading.                        
                      
                          Clamps used to fix walkways are rusted.                        
                      
                          Fans and filter in an inverter were heavily
soiled.                        
                      
                          Some modules are shaded by a taller section of the building.                        
                      
                          Shoeprints found on modules.                        
                      
                          IR analysis shows presence of hot cells.                        
                      Impact on Performance
                        Heavy Soiling                        
                      
                      
                          The system performance was affected by soiling loss of 3.5%, estimated from IV curve measurements.                        
                      
                          Estimated Loss
                        
                        
                            ≈ 3.5%
                          
                        
                        Cell Cracks                        
                      
                      
                          The EL image reveals cracks and isolated parts from broken cells. All modules tested for EL revealed isolated parts. Power loss estimated from mechanical damages is expected to be around 3%.                        
                      
                          Estimated Loss
                        
                        
                            ≈ 3%
                          
                        
                        Underperformance                        
                      
                      
                          Based on the IV curve measurements, the estimated underperformance is 7.7% for the measured modules.                        
                      
                          Estimated Loss
                        
                        
                            ≈ 7.7%
                          
                        
                        Near Shading                        
                      
                      
                          Simulations from PVsyst revealed near shading losses to be 1.95%, and a 1.34% loss from reduced heat dissipation.                        
                      
                          Estimated Loss
                        
                        
                            ≈ 1.95%
                          
                        
                    Total Estimated Energy Loss
                  
                  
                    ≈ 19.72%
                  
                Proposed Solutions
                          The cable layout shall be optimized, the minimum bending radius shall be 10x the cable diameter, and cable racks shall be used.                        
                      
                          Rails used currently of around 30 mm height shall be replaced with ones that offer an effective clearance of 100 mm to facilitate better air flow and improve system performance.                        
                      
                          Open shaft holes shall be covered since they pose a several threat to the O&M personnel.                        
                      
                          A proper O&M plan shall be established that includes instructions on module handling.                        
                      
                          A re-sorting shall be conducted to have modules with isolated parts in the same string or at least same MPPT.                        
                      
                          A re-stringing of modules shall be conducted to have shaded modules in the same at least same MPPT.                        
                      
                          A weather station, or at least an irradiation sensor on the module plane shall be installed so that the performance of the system can be properly determined.                        
                      
                          Faulty clamp fixations shall be properly fixed, and clamps with faulty threads shall be replaced. Rusted clamps should be replaced if possible. To prevent such problems, metal objects vulnerable to corrosion can be painted with zinc.                        
                      
          